30 Years!

I just got back from a trip to Hawaii, the Big Island.  The occasion?  My wife and I celebrated our 30th Anniversary!  Yep, 30 years ago she took vows with me.  We’ve had our share of ups and downs but this trip was definitely one of the ups.  Five years ago we went to Maui with our family for our 25th Anniversary.  This time around it was just Cristy and I.

We landed at Kona, rented a 4WD Jeep and drove up to the North side of the island.  We stayed at a B&B in Kukuihaele about 1/4 mile from the Waipio Valley.  The house was basically a studio bungalow and the scenery was absolutely stunning.  The house is set on the side of a hill overlooking the Pacific Ocean.

For 5 days we gorged ourselves on fish and fruit, visited beaches, gardens, waterfalls and ate more fish and fruit.  The reason for the 4WD Jeep was so we could visit the Waipio Valley and beach.  The drive down the road was quite a thrill.  Steep mountain road grades in the Western US are like 6-8%.  This road was a 25% grade!

Since pictures are worth far more than words…

Blasts From The Past

This past week I’ve had two different people from my past make contact with me.  An old neighbor spotted me on Facebook and reached out to me via Messenger.  We had a brief back and forth exchange and that was it.  The other was a coworker from a previous employer.  She added me on LinkedIn.  I reached out to her via LinkedIn’s messaging system and again, there was a brief exchange and that was it.

Kind of disappointing on both counts.  I would really like to reconnect with both these folk and see how their life is going but they seem content with just superficial contact.  They just wanted to know that I was still out there somewhere… and that’s it.  So much for social networking. 🙂

That’s okay.  I’m glad to know they’re both still out there somewhere too.

Good News!

In my previous blog entry I wrote about my engine woes.  I sent the photos to Rolando Santiago at Six Chuter who took a look and informed me the piston was toast.  He and Doug Maas consulted with J-Bird Engines (the engine manufacturer).  J-Bird asked for the engine to be sent to them so they could take a look.  To their credit, the guys as Six Chuter paid the cost to ship the engine back!  Once the engine arrived, the guys at J-Bird knew exactly what happened.

You see, there are exactly two belts on this engine.  Both of them are fan belts… more or less.  One belt is on the rear of the engine and connects the crankshaft to the propeller.  It reduces the RPM of the propeller because the prop isn’t designed to turn at 6500 RPM.  The other fan belt turns an actual cooling fan at the front of the engine.  Now there are sections in the engine manual that describe tightening these belts.  I dutifully checked the belt tension on the prop, but missed the huge page in the manual saying how important it is to adjust the tension on the fan belt!

When J-Bird dug into the engine the first thing they noticed was how loose the fanbelt was on the cooling fan.  And yep, the front piston was in the worst shape.  Problem found.  The engine was overheating due to poor cooling.  Totally my fault.  But here is where the AMAZING customer service part of the story comes in.  I was told the engine would be rebuilt at NO COST to me whatsoever.

Now, gentle reader, I don’t know how much you know about aircraft companies but Six Chuter is an anomaly in aviation.  Most aircraft companies would have said “Uh, user error, you need to pay the cost to fix your engine.”  Six Chuter did not do this because they believe in their products.  They stand behind their products and the components that go into their products.  Six Chuter is run by people of integrity and truly believe they are held accountable to God for everything they do on this earth and it shows.  I cannot say enough about this company.

So back to the engine.  They are going to rebuilt it from the crankshaft up and it should hopefully be shipped back to me next week.  I’ll post more updates on the re-install and next steps on the engine when I get it back.

Morning P3 Test Flights

I’ve been doing lots of tweaks and testing of my engine on the ground but haven’t flown it much.  I changed that this past Friday and Saturday mornings.  Friday morning I flew with the 10 degree prop blocks.  These set the propeller pitch to 10 degrees.  I found that throttle response was good but because of the fine pitch of the prop climb rate was reduced and I found myself at almost 6000 RPM just to maintain level flight.  That only gave me a couple of hundred RPM more to climb with.  Not a good feeling.  Also the engine cylinder head temperatures were running too high at 400 degrees.  Even worse feeling.  However throttle response and smoothness were much improved as was exhaust gas temperature.

Friday night after work I put the 11 degree prop blocks in.  I test flew these Saturday morning.  In all honesty I didn’t notice much difference in the way of climb performance but CHT was lower which was good and EGT was also lower which is very good.  I did notice a little ‘bogging down’ of the throttle in one particular RPM range but it wasn’t too bad.

For next week’s test flight have have moved the carburetor jet needle to the number 2 position.  This will make it run slightly leaner which may cause EGT to rise.  I’ll have to watch that.

Because there are so many parameters to change it’s all started getting mixed up in my head.  To that end I’ve started a spreadsheet to track and measure all my changes.  I should have done this in the beginning.  I’ll put the link below in case anyone is interested.

https://docs.google.com/spreadsheets/d/1X_E330q6iU6X_8-54gjdI0Xuz_Gk5UPr6Od_Bf1Eomk/edit?usp=sharing

I’m also going to take a page from one of the blogs I follow.  He always leaves a song linked to the end of his blog.  I like the idea.  So cruise on into your Sunday evening with the smooth sounds of Tom Middleton…

Life 3.0

Life 1.0 was pre-marriage.  Being born, growing up, going to school and college.  Life 2.0 was entering the workforce, marrying Cristy, buying a home, adjusting to each other.  Then came 2.1 and 2.2, my son and daughter.  Now that they have both more or less moved out we come to Life 3.0.  Empty nesters.

Should I feel guilty that I feel excited for my kids?  I’m excited they get to start experiencing the world on their own.  I think of all the adventures I had when I was my kids’ age and I can’t wait for them to begin their own.  I’m excited for them.

And I’m excited for Cristy and I.  We can start making plans for just ourselves again.  I love my children and I will always want them in my life.  But I love the life that Cristy and I can lead together now too.  And I can’t wait.

I Think We’re About There

So the last two weeks there has been little in the way of flying and a lot in the way of carburetor tuning.  We’ve been tweaking jet needle settings and even replacing jet needles but the one change that seems to have worked wonders is repitching the prop.   Six Chuter sent me two more sets of prop blocks to repitch my prop.

The blocks are basically triangular blocks of carbon fiber, similar in appears to a door stop – sort of shaped like a right triangle.  The long edge is precisely set at a particular angle.  You wedge the prop between two of these blocks and then place it in the propeller hub and that sets your blade angle.

The current spacers I have are set at 12 degrees.  I tried the 11 degree blocks but that didn’t seem to make any difference.  When I put the 10 degree blocks in I got much better RPMs and cooler temperatures, so much so that I put my original jet needle back in and back at it’s original setting.  I’ll try a test flight on Saturday morning and we’ll see how it it works out.

P3 Lite Carb Tuning Continues

I took the test flight I wrote about in the last article.  I had moved the needle clip to the top-most position on the needle, effectively leaning the mixture.  The resulted in PERFECT throttle response.  However, it also resulted in much higher engine temperatures.

No bueno.

I spoke to the folks at Six Chuter again and they are going to send me a different needle for my carburetor.   They are also going to send me some new pitch blocks for my propeller.    They believe the prop may not be allowing the engine to turn as fast as it should.  I’m only getting about 6100 RPM static.  They believe it should be closer to 6500.  I’ll be trying the new spacers which will allow the prop to spin faster.  This will cause the engine to work less hard to spin the prop as well.  I’ll do another test flight once the spacers come in.  If the spacers don’t correct the heating problem then I’ll try the new carburetor jet needle.

Six Chuter has been very responsive and I appreciate the factory support I’m getting.  Great company!

P3 Lite Carburetor Testing / A Name

I have been having trouble with the throttle response of my P3.  I called the factory support line and talked to their engine guru.  He suggested that I run the P3 on the ground, throttle up until I get into the problematic RPM range, and then give it a little shot of prime.  (The primer shoots gas directly into the carburetor and is generally used only during starting.)  The thought was if I gave it some prime, and then engine bogged down, then I’m running too rich, if the engine revs up, then I’m running too lean with the stock settings in the carburetor.  I tried the test and it bogged down big time.

Six Chuter factory support recommending I change the clip position on the jet needle.  With out going into carburetor theory the jet needle controls how much gas the carburetor delivers to the engine.  Moving the clip up makes the engine run leaner, moving it down makes the engine run richer.  I moved it down first, and the problem became worse.  I moved the clip up and throttle response was good throughout all RPM ranges!

I did have a momentary scare when I saw that there was a split in the clip on the jet needle.  I had never noticed it before but was assured it was completely normal and was part of the design.  Six Chuter factory support assured me this was normal.  And a friend of mine who has an extensive ultralight history assured me this was normal.  In fact, he sent me an article by Chris Wolf on rebuilding the Bing 54 carburetor which has this excerpt:

If you look closely at the E CLIP, you’ll see that it has a break in the
metal, right next to the curved part of the clip that snaps around the body
of the JET NEEDLE.  This is as it should be.  Rest assured that you didn’t
break the clip when you pulled the JET NEEDLE out of the piston.

http://www.powerchutes.com/bingcw.asp

Well that’s exactly what I did.  I dropped the clip on the ground and thought I broke it!  So glad Jim Volk sent me that article.

Now that I have the carb adjusted properly I’m going to give it a test fly tomorrow and see how it works.  I’m hoping this cures the problem and I can start working on my landings again.

A Name

I’m not big on naming inanimate objects.  I’m not good at it.  However, when a fellow P3 pilot suggested that since I used to work right outside the gate to Moffett Field and I had P-3 Orion Sub Hunters flying overhead all day, and since I was working for the company that manufactured these airplanes, Lockheed, that I call my P3… Orion.  And a name is born!  This same fellow also quipped that I should check the belt drive on the propeller from time to time, as he put it, don’t for get to check Orion’s belt!

P3 Lite Status Udate

Here’s just a quick video with a status update on my P3 Lite Powered Parachute from Six Chuter.  Still enjoying this little beast.  Have worked out a couple bugs and have just one more to go.  Great little machine!

And Even More Flying

After a REALLY hectic week at work it was great to unwind out at New Jerusalem flying with my buddy Joey.  He’s actually the one that suggested I try PPC rather than PPG.  Joey was already set up and ready to go by the time I got out there.  The air was calm and cool.  Joey launched and I finished getting my PPC ready to go.  I bucked in, fired up my engine and 100 feet later I was climbing into the air.

We flew out over the river but it got a little bumpy that direction.   We were probably hitting a little wind shear since the wind was starting to slowly pick up.  I turned south and my ground speed went from 17 MPH to 42 MPH.  I messed around checking my throttle response (I had adjusted the carb earlier in the week).

I flew back to the airport and could see that the wind was picking up.  At this stage in my PPC flying I elected to go ahead and land and call it a day.  After packing up I ran into a group of balloonists.  As luck would have it they had been taking pictures of Joey and I.  So I will leave with with some of the pictures they took.